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Post by Joe on Jun 4, 2011 19:12:17 GMT -5
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Post by louross on Jun 4, 2011 19:24:34 GMT -5
ummm. jeeze. lr
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Post by Tom Goodrick on Jun 5, 2011 7:00:10 GMT -5
Bad luck for the runner and bad forward visibility for the pilot. He solved his landing problem. I suppose the loss of the prop pushed the CG back a bit and raised the nose.
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Ed Burke
Member
Healthy living is fine, but it's having fun that keeps us going!
Posts: 433
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Post by Ed Burke on Jun 5, 2011 18:57:36 GMT -5
That poor guy, if only he had been having a lazy drink in the bar, or asleep. He would have had no idea he was in trouble. I feel for the pilot who is blameless but has to live with it.
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Post by Tom Goodrick on Jun 5, 2011 21:42:07 GMT -5
So I thought there was something strange about this story. It happened at Hilton Head, SC and was reported in the Dallas newspaper on 17 March, 2010. Why are we discussing it now?
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Post by flaminghotsauce on Jun 6, 2011 10:13:25 GMT -5
Good catch Tom. Even interesting even if it was March 2011. Why did it take so long? Why now?
I must say I distrust all major media, AP and Reuters are at the top of my "Must Verify" list. And they are the majority of supply for newspapers and stuff.
I'd say they are in dire need of distracting news.
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Post by Joe on Jun 6, 2011 23:00:41 GMT -5
Wow, oops. Someone mentioned it to me that same day as if it were a current news item, so I Googled it assuming it was recent news. I didn't even see the "Published March 17, 2010." My fault, not AP's, flaming.
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Post by Tom Goodrick on Jun 7, 2011 9:29:41 GMT -5
I just checked the NTSB records. After all this time they have only issued a brief statement of the facts. The aircraft was constructed by the pilot so there seems to be no need to investigate why the prop came off.
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